my brother is no longer taking the LCR....... the insurance company are wanting crazy money to transfer his policy over for the remaining 4 months.... he was looking forward to the swap aswell.
so the car is now officially up for sale.
yesterday i fitted the correct n75 valve after dave @ sere motors sent the correct one out this time lol, car is running a million times better now
also removed the pumped rear weitec shocks and fitted the stock ones back in temporarily til replacement weitecs are sent back out
also stripped the passenger side rear door down, turns out there was a loose connection onto the pcb for the central locking unit, all is now functioning again and i now have 4 fully operational doors again
only after months and months of only having 3 :lmao:
the car would now be sitting ready to go now...... but when i was having a nosey at the front pads to check the wear i noticed the inner CV boot on the nearside was split
so i went round to check the offside one and it was badly worn too
so will price up a couple of CV boots and will get them fired on at the 1st oppourtunity, then i'll be ready to rock and roll with finding the LCR a new home