Genuinely no
stickers, or any residue of them.
So update. Unfortunalty, my camera died after about 4 pictures.
Basically, all was ok, until, it came to fitting the downpipe. the 2871r is longer in a dimension somewhere meaning the relentless manifold and downpipe fouled each other. so a bit of 'tolerancing' was required. a small dink in the manifold and about 10mm of downpipe plange was cut away to allow fitment.
This has meant its making contact with the body somewhere which is annoying as I cant see it, so it's coming off again tomorrow for more 'tollerancing'.
Started up with the new clutch and it is genuinely silent. Ive not seen a SMF conversion like this until now.
Clutch feel is lovely, very OEM.
Turbo wise. Well. OH MY GOD. Spool is just the same as the K04, but, its holding 26psi at 75% throttle at 5000rpm Before I Bottled it. as my laptop didnt standby and had gone flat again.
Laptop charged up today, +10% fuelling, and -5* of timing to make it run a bit safer when on boost.
Did a quick log, it started to run lean at 6300 so aborted, however just as i aborted the highest MAF reading was 269.11g/s (336.25bhp)
Its going to be a quick one
N75 is now unplugged, back to 10psi. this is going to be a long month until mapping